Commencing the Build

Well it took a while but I’ve finally started.

 

Painting

First up was to paint everything. This was a fun task except for all the cleaning up – Yeich!!

Did three coats and used a good quality epoxy paint called – White Knight. Ive painted it white, hopefuly it wont look too shitty once it gets a bit dirty. A darker colour would be more sensible and I am sure Ill regret the colour selection later – but I'm hoping it will look good as a background to the red that I will be painting the outside of the car. I also plan on stripping the car back to components once finished and touching up all the scratches nicks and adjustments that I am sure I will make on the way through.

 

Aluminuim Panels

Next was to clad the aluminium around the outside of the chassis.

Now this was fun – felt like I was starting.

No big dramas. I put my panels on the Outside of the chassis but I have since seen one other car with the panelling on the inside. Both seem to work OK.

It was at this point I had 2 months travelling away from home – so NO work got done!!

But during this time I bought another car, which I had to enjoy while waiting for the Westfield J .

 

Steering Column

Putting the steering column in requires some imagination!! The instructions are for a ford Escort or Allegro column (whatever that is?) and I was using a Toyota Corolla steering column. I actually had two columns so I had a bit of a play with the first one to get it right.

 

I purchased the nylon bush for the end of the shaft from John Henderson (the NSW Westfield agent) and put it in the end of the shaft to stop it rattling around. The next problem was to determine how to fix the lower end of the shaft in the footwell hole. I decided to use the existing Toyota mounts inside out. By reversing the plate I put it on the outside of the firewall with the rubber face against the firewall. With very minor modification of the firewall hole I was able to mate it up the original components and it will be watertight as well.

This created a small problem however (like all self modifications!!) The shaft was further down the tube so I would clear the Toyota plate on the bottom of the column tubing. To adjust this I shortened the steering wheel end of the tube by 25mm, adjusting the ignition switch orientation in the process. This actually is good as it puts the steering wheel closer to the dash, which suits me as I am not planning on using the stalks switch indicators.

 

Suspension

A piece of cake 4 hours and it was finished!! I have to admit I thought this would take longer than it actually did but it is relatively easy to do. One thing that is required at this stage is a pair of spring compressors, which are cut down to fit between the coils of the springs. My neighbours were also an essential element as I ran out of fingers. I ended up using SPAX adjustable platform shock absorbers. I have been told that they are not as good as AVO due to the inability to be rebuilt, but price dictated this purchase. I will be able to give feedback as to longevity later!

 

The first mistake occurred here. I installed the diff in the housing with the larger MKII Escort flange (4") instead of the MKI Cortina Diff Flange 3 3/8". I will need to pull this out and put the correct one in – Ho Hum.

 

Nutsert Tool

I have given the Nutsert tool a special section, as it is the most useful tool I have EVER bought. This is a big call, but I suspect that most people will find this the same. As well as the Westfield I have used it on household repairs and on other cars. $135.00 well spent!!

 

Handbrake Take 1

I fitted the handbrake to the tunnel top using the Nutsert tool. When I tried to hook up the existing handbrake lever I discovered that the MKII escort handbrake mechanism WOULD NOT WORK. The main reason is that the panhard rod is in the way, so I cut off the brackets for this setup and started the thinking process for an alternative.

 

Brakes

I replaced the disk pads on the front and shoes in the rear drums and overhauled the slave cylinders. Then measured up the brake lines. The master cylinder that I had looked OK so I decided to use it without overhauling that. Took the measurements to the brake place and they made them up for overnight. Bought a brake line bending tool and installed them without much difficulty. And not a single leak out of the line junctions. One note here is that there are 3 types of master cylinders from TD Cortina. Mine is a two-outlet system with 12mm outlets. The other options are a three port with 12mm outlets and a third alternative of two outlets with a 10mm and 12mm. With my master cylinder I needed a t piece for the front two brakes. If I was searching again I would by the master cylinder with three outlets, which does not require the additional T piece.

The brakes pressurised up nicely and we then took the car for a spin. My neighbours pushed me down the road for about 100m and then a three point turn and back again!! A two human powered car is no speed machine I can tell you!!

 

A small problem that occurred was that the master cylinder leaked out the back. This was fixed simply by installing a new kit. The bore looked OK so no honing was required. I suspect that the old rubbers had dried out and lost their pliability while it was out of service.

Also Bought a pair of slotted and cross drilled disc rotors for no other reason than I liked the look of them?! Silly I know - But they will look great :-)!! >

Trial fit Body

The fibreglass body fitted over the car nicely, no major problems were expected or experienced. The fit was Ok. One thing to note is that you actually need to cut the bonnet off as it is about an inch too long. This is done I presume so you can have the nosecone mounted further forward.

 

Dash Panel

I could see from early on that my dash that I made earlier was not going to fit. There is just NO room around the steering column for anything but a 75mm gauge. No to be outdone I continues searching. While I was pulling a steering universal from a triumph 2500 PI I noticed that the dash comprised of round smiths gauges. These looked the part, especially the fact that a separate "gauge" existed with 8 pieces of pie, for all the functions like indicator signals, ignition light, brake warning etc. etc. etc.

While I was doing this I extracted the entire wiring loom and decided that this would form the basis of the harness I would use in the westie. I could see that using the gauges out of the Triumph would also save A LOT of time in wiring up the gauge harness!!

When creating the dash panel itself, I considered putting the panel on the outside of the scuttle (conventional place) and on the inside of the scuttle. I decided to put it on the inside as this would them remove the necessity to finish the edge of the panel.

I have secured the panel using 5mm stainless cheese head bolts through the scuttle.

 

Engine

The moment of truth!!

Will it or wont it. I fitted the clutch up to the flywheel (thick side towards the gearbox) and that happened with no problems, (A good omen?) and bolted the gearbox up to the engine. The next morning, I was so anxious to get it in – I decided to go to work late one morning and started at 6:30am. By 8:00 am it was all over the engine was in!! The gearbox was bolted up to its mounting and everything was rosey!. Too EASY!

A couple of niggles along the way, which were easily sorted.

 

  • Take the alternator off;
  • Remove ALL external water plumbing;
  • Take the support brace between the inlet manifold and the block off;
  • Move the Master Cylinder back about 15mm.

The fourth thing was the most difficult as I had to undo the pedal box and drill a couple of holes 15 mm back from the original. I then had to let the master cylinder fluid out and grind the bottom of the mounting flange to enable it to clear the firewall bracing. This took a sum total of 15 minutes however. Anything that holds me up for less than and hour is not a problem its only a nuisance. (Incidentally visitors fall in this category too. A less than 1 hour visitor is a nuisance; a greater than 1 hour visitor is a problem!!). The reason that I had to move the master cylinder is that the air inlet ran into the master cylinder. This is not a problem with the 88kW motor apparently.

A good point however is that the alternator fitted without modification to the brackets. It appears that the 100kW 4AGE alternator fits Ok, but the 88kW 4AGE alternator brackets requires modification. The only thing I did have to do was shorten the peg that the charge wire attaches to. Oh and of course I had to re-pressurise the brakes (I hate the smell of brake fluid.)

 

This is a turning point in the construction. The next thing to do is the wiring harness, and I suspect that the easy to do jobs have run out!!

 

Next Page – Wiring Wiring and more Wiring!!

 

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